Jetting
#11
#12
#13
It's clean unless there's a passage blocked I'm unaware of. Seems odd I don't know what I'm missing. I've rebuild dozens of carbs and jetted them never had an issue like this but this is also the first time I've ever had a Keihin CV. I'm open to suggestions. It has a lot of new parts, slide, cvp jets and needle.
#14
Originally Posted by 98hotrodfatboy
Is it possible that your choke circuit has something to do with it. That would explain no change at idle with the screw and lack of power in the top.
Last edited by br549A1; 04-15-2017 at 03:27 PM.
#15
Kp, i wish i had more knowledge on that carb. I've never messed with one but if you think of the statement you made earlier "i turned the idle screw in all the way in and it idled fine" that right there should tell you that it's sucking fuel from somewhere..... You might have to take it back apart. And for what it's worth i thought the plugs were way too black (rich). I wish i could be of more help.... Sorry man....
Last edited by 98hotrodfatboy; 04-15-2017 at 07:22 PM.
#16
#17
No didn't replace the mixture oring. I looked at it last time it was apart it looked fine. I thought I was rich running before I pulled the plugs but I thought the plugs looked lean. Am I completely wrong on the plug reading? I'm still at a loss with the 4500 plus. I ended at 46 pilot due to coughing off idle. It used to cough hard off idle leaving stop signs. I'm not sure where am at now.
Thinking of what I've replaced on it. I've replaced everything except ignition box and coil but both test fine. With cam and good compression readings I don't see any reason why I shouldn't be pulling to rev limiter. I think I have a carb issue but I'm confused as to what it is. Also the float was set to 11mm.
Thinking of what I've replaced on it. I've replaced everything except ignition box and coil but both test fine. With cam and good compression readings I don't see any reason why I shouldn't be pulling to rev limiter. I think I have a carb issue but I'm confused as to what it is. Also the float was set to 11mm.
Last edited by br549A1; 04-15-2017 at 08:10 PM.
#19
Not so sure the 3010 can pull past 5300 rpm. It's a good cam but not for that range. the 3020 would do a better job but the Woods W6 would out do the 3020.... for a cam only upgrade.... If you're going to replace the carb the best thing you can do is go to an S&S E..... It's easier to tune..