EVO Rebuild
#1
EVO Rebuild
What was supposed to be a simple rebuild to fix a case oil leak has turned into anything but. The original plan was to split the cases,replace the crank bearing, put the bottom end back together and seal the cases,go back with 9.5:1 pistons, an EV27 cam and rework the heads.
When my indy tried taking the pinion nut off, the nut wouldn’t come off with the tool and started rounding the nut and stripping the tool. He had to machine the tool down and weld it onto the pinion nut in order to get the pinion nut off. Once the cases were split he found that it had a shovel head crank instead of an Evo crank although they are the same spec, just a different taper on the pinion shaft. He said there was too much side play in the connecting rods.
My guess is that something came apart in the bottom end and the previous owner slapped it back together just to get it running and get rid of it.
The crank was sent to Darkhorse CrankWorks. Once they took the crank apart, they determined that the inner crank bearing was shot and had to put oversize bushings and pins in the connecting rods. The cases were sent to Darkhorse and they repaired the Timken/Main bearing bore as main bearings were loose in case. Darkhorse also line bored and lapped the cases and put the bottom end back together and sent it back to my indy.
Once Kevin got the bottom end back, the heads were ported and polished, 1.90 intake and 1.610 exhaust valves, cylinders bored .020 over (they were already .010 over), KB forged 9.5:1 pistons, EV27 cam, new S&S lifters, adjustable pushrods since the heads were milled, new S&S breather gear. Daytona Twin Tec ignition and single fire coil.
I just picked it up today and it runs really good. Nice and smooth due to the crank work that Darkhorse did.
Link to initial startup
When my indy tried taking the pinion nut off, the nut wouldn’t come off with the tool and started rounding the nut and stripping the tool. He had to machine the tool down and weld it onto the pinion nut in order to get the pinion nut off. Once the cases were split he found that it had a shovel head crank instead of an Evo crank although they are the same spec, just a different taper on the pinion shaft. He said there was too much side play in the connecting rods.
My guess is that something came apart in the bottom end and the previous owner slapped it back together just to get it running and get rid of it.
The crank was sent to Darkhorse CrankWorks. Once they took the crank apart, they determined that the inner crank bearing was shot and had to put oversize bushings and pins in the connecting rods. The cases were sent to Darkhorse and they repaired the Timken/Main bearing bore as main bearings were loose in case. Darkhorse also line bored and lapped the cases and put the bottom end back together and sent it back to my indy.
Once Kevin got the bottom end back, the heads were ported and polished, 1.90 intake and 1.610 exhaust valves, cylinders bored .020 over (they were already .010 over), KB forged 9.5:1 pistons, EV27 cam, new S&S lifters, adjustable pushrods since the heads were milled, new S&S breather gear. Daytona Twin Tec ignition and single fire coil.
I just picked it up today and it runs really good. Nice and smooth due to the crank work that Darkhorse did.
Link to initial startup
Last edited by Tony_N; 07-14-2016 at 06:06 AM.
#3
Join Date: Jan 2011
Location: Haslet Texas
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#4
Thanks Maxdog2
The crank wasn't replaced, Darkhorse replaced the bearings, bushing and connecting rods and balanced it. Had I known the extent of what was done, I would have gone with the stroker kit. Every time I turned around, it was something else that just kept adding up. Hind sight, I could have gone with a 111 S&S for less than I had in this rebuild.
#6
Join Date: Jan 2011
Location: Haslet Texas
Posts: 20,999
Likes: 0
Received 4,317 Likes
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1,946 Posts
Thanks Maxdog2
The crank wasn't replaced, Darkhorse replaced the bearings, bushing and connecting rods and balanced it. Had I known the extent of what was done, I would have gone with the stroker kit. Every time I turned around, it was something else that just kept adding up. Hind sight, I could have gone with a 111 S&S for less than I had in this rebuild.
The crank wasn't replaced, Darkhorse replaced the bearings, bushing and connecting rods and balanced it. Had I known the extent of what was done, I would have gone with the stroker kit. Every time I turned around, it was something else that just kept adding up. Hind sight, I could have gone with a 111 S&S for less than I had in this rebuild.
Gotta love a sleeper!!!!!!
#7
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#8
Your bike turned out great! That thing looks and sounds right. Even if you're into it for more than you bargained for, looks like a winner from here.
#9
#10
The money's spent. The bike runs sweet as hell. By your account the build was done right. Seems like a great day, in Buford, Ga., for a ride. And I agree those all black cylinders are the ****. I'm thinking about doing a bolt-on 'big bore' kit when I get my base gaskets done. I was looking at black with highlights cylinders…but seeing your black ones…that'll be the ticket, now.
Alan
Alan
Last edited by AlanStansbery; 07-14-2016 at 07:42 PM.